This project began with my purchase of a partially working Onewheel plus. I was looking for a battery project with the purchase of this board so was not upset to find thats its BMS was not working. My first goal was to build a battery that could replace the original battery with upgraded range and equal or more power.
My first battery, lets call this v1, was a 14s3p INR21700M50LT pack. I had no expierence building onewheel batteries
(or batteries at all) and was fairly disconnected with the aftermarket community. To summarize this battery was a disaster waiting
to happen. In order to fit this many cells in the frame I had to put the BMS on top of the battery box, in the footpad.
The first thing to fail on this build was the welds. I used a cheap battery spot welder and had no prior expierence
building batteries so my connections were weak.
Since I used a smart BMS on this build I first noticed a cell dropping in voltage much faster than the rest. Once disecting this battery I found several loose welds likely to have caused the cell's voltage drops.
After a bit more research I started planning my next battery build. This was a 14s2p pack using Molicel P42B's. For the BMS I used a Daly 14s smart bms. I had also upgraded to a Glitter 801D spot welder for much stronger welds. I used 0.2mm nickel strips for all welds. The first falure of this build was a cell going out of balance. Since it was cell 14, the last in the string, I simply replaced that parallel group with extra cells I had on hand. I also swapped my bms to a JBD 12-17s smart BMS for better active balance.
There were a few major things I did wrong on this build: I did not use any fishpaper, I used a charge/discharge BMS, and the balance wire were routed very poorly.
Since I was still new to battery building I was not aware of the importance of fish paper. I placed the cells tight to each other, using only the welds to bind them until I taped them all together. While this seemed to work, it was difficult to assemble and not properly designed for the vigorous vibrations of onewheeling. One of my theories of the cause of v2's second bad cell and ultimate falure was the lack of fish paper. Several cells showed signs of corrosion, and a few had parts where the nickel strips had worn through the battery heat shrink making contact with the metal of the cell.
Although never proving to cause any problems, the balance wires were routed in such a way that they over lapped each other many times. In a tight build like a onewheel this could cause a short over time with many vibrations.
The next upgrade to my board was replacing the original onewheel plus controller with a Little Focer 3.1 Vesc
compatible ESC. The Focer came in a kit and was fairly straight forward to install. I 3d printed a box using high
speed TPU. I decided on HS-TPU since it wouldn't crack under heavy and constant vibrations. I switched the wiring
in the battery box so that the BMS acted as a charge only BMS, making it so the Focer pulled power straight from the
battery. This created no risk of the BMS dropping the board if thinks there is a problem (this happened to me once).
The BMS also does not need to carry near as much current in this configuration.
There were a few aspects of this conversion I was not satisfied with at the end. The main was the large connector from the battery box to the controller box. It is a 16-pin plug that carries battery current (charge and discharge) and rear LED signal and power. The connector fits loosly and has a easily breakable clip to hold it in place that left me feeling a bit un comfortable. Similarly the motor cable was an almost identical 6 pin connector that I had the same feelings for. The other part I did not love about this design was the TPU box, while it never did crack it was too flexible and felt like it never created a reliable water seal around the connectors.
After I graduated School I embarked on yet another board renevation, and the biggest yet. The main goal was to upgrade to an 18s2p pack from my 14s2p pack that was having yet another out of balance cell. This time I was determined to do everything right and not have any more battery issues. On this rebuild I did three major upgrades:
There are a few other smaller aspects, lights, fender and footpads that I updgraded on this version. The lights I still, as of 10/9/25 have not fully got working. The partial fenders that I had 3d printed, broke and I will likely just buy the drop top from TFL My foot pads I printed with HS-TPU and used trail grip tape from TFL.
At this point I have an original future motion motor and rails. Everything else is aftermarket. A few resources I used for this build are:
Now that I have finished I'll give some reflections. My total amount spent in parts that are still on the board, or were not resellable or reusable, probably sits in the ball park of a Onewheel GT or my preferred the Fungineers X7 or Floatwheel's ADV2. My board would to the best of my knoledge out-torque the GT but be fairly comparable to the X7 or ADV. Looking back, if I just wanted a high-speed, high-torque onewheel I would buy a Fungineers X7 Long Range. If I wanted a project and to learn I would build another board but from scratch, using a superflux motor from Fungineers and WTF rails from TFL. (Instead of the two remaining future motion parts I have on my board).